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JK Lakshmi Cement Limited Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
JK Lakshmi Cement Limited Global Energy Management Implementation Case Study

Successfully achieved 14.82% reduction in Specific Energy Consumption (SEC)

This case study describes how JK Lakshmi Cement achieved a structured platform for energy consumption, energy conservation, and energy management activities by implementing Energy Management System (EnMS), ISO 50001. They achieved a total energy cost saving of Rs 903 million, with an investment of Rs 2832 Million and an average payback period of 38 months.

Hitachi, Ltd. Infrastructure Systems Company Omika Works Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
Hitachi, Ltd. Infrastructure Systems Company Omika Works Global Energy Management Implementation Case Study

Omika Works improved 15% of energy performances

This case study describes how Omika Works reduced 23% of the contract electricity, 15% of CO2 emissions and 5 million yen/month of electricity costs by means of visualizing the electric power, making the basic unit of it including the smart next-generation factory plan and promotion of the improvement measure of the energy use efficiency by EnMS. Omika Works is the central base of Hitachi, Ltd. Infrastructure Systems Company which promotes a social innovation business of an energy, an aquatic environments, a mobility, and an industry.

F-TECH INC. Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
F-TECH INC. Global Energy Management Implementation Case Study

Faced with energy shortages after the earthquake, they recognized the importance of energy management

This case study describes how the Kameyama Plant reduced CO2 emissions of 1,379 t-CO2 by 27% (compared with FY2010). They reduced 182 t-CO2/year, and saved 8.8 million yen through energy saving activities such as paint circulating pumps inverter control and LED installation at stamping area.

PT. Pertamina Hulu Energi Offshore North West Java (PT. PHE ONWJ) Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
PT. Pertamina Hulu Energi Offshore North West Java (PT. PHE ONWJ) Global Energy Management Implementation Case Study

By Implementing EnMS, 5% Energy Savings has been achieved per year

This case study describes how PHE ONWJ became the only subsidiary of PT. Pertamina (Persero) to implement Energy Management System (EnMS) ISO 50001. By implementing low and no cost Energy Conservation Opportunities (ECO’s), PHE ONWJ has reduced its energy consumption by 5% (2014) and 3% (2015).

PT Indah Kiat Pulp & Paper Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
PT Indah Kiat Pulp & Paper Global Energy Management Implementation Case Study

The first paper mill in Indonesia to be awarded ISO 50001 certification

This case study describes how IKPP Tangerang became the first paper mill in Indonesia to be awarded ISO 50001 certification. IKPP Tangerang succeeded in reducing energy consumption from 9.32 GJ/TP in 2011 to 7.91 GJ/TP in 2015.

PT. APAC INTI Corpora Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
PT. APAC INTI Corpora Global Energy Management Implementation Case Study

Conducting energy conservation programs since 2006

This case study describes how PT Apac Inti Corpora started implementing the global energy management system of EnMS-ISO 50001:2011 and certification was achieved in June 2014. Since the implementation of these conservation programs, they have reaped rich benefits in terms of cost, culture, quality, productivity, safety, moral and business efficiency.

Nissan North America, Inc. Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
Nissan North America, Inc. Global Energy Management Implementation Case Study

Automaker improves energy performance 25% over six years with SEP

This case study describes how Nissan worked with the U.S. Department of Energy’s (DOE’s) Advanced Manufacturing Office (AMO) to implement an energy management system (EnMS) that meets all requirements of Superior Energy Performance (SEP) and ISO 50001. At its vehicle assembly plant in Smyrna, Tennessee, the company established an energy baseline and assessed opportunities to save energy within its major energy-using systems.

New Afton Mine Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
New Afton Mine Global Energy Management Implementation Case Study

New Afton is the first mine in North America to implement ISO 50001

This case study describes how New Afton Mine started production in June 2012 and received ISO 50001 certification on March 31, 2014. With a number of prestigious energy management related awards received over the past few years, New Afton continues to set an example of what is possible as a result of passion, drive and commitment.

Mutua MadrileƱa Automovilista Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
Mutua MadrileƱa Automovilista Global Energy Management Implementation Case Study

Low cost, high impact. Going beyond social and environmental responsibility: energy management as a commercial and business asset

This case study describes how Mutua Madrileña implemented an ISO 50001 Energy Management System (EnMS) that brought their energy performance to a new level. After two years in operation, they have saved 5,891,444 kWh in total for 14 buildings, 18.4% of total energy costs.

HARBEC, Inc. Global Energy Management Implementation Case Study

Wednesday, May 18, 2016
HARBEC, Inc. Global Energy Management Implementation Case Study

Specialty plastics manufacturer improves energy performance 16.5% to earn Platinum certification in Superior Energy Performance

This case study describes how HARBEC, Inc. worked with the U.S. Department of Energy (DOE) Advanced Manufacturing Office to successfully implement an energy management system (EnMS) that meets all requirements of ISO 50001 and Superior Energy Performance® (SEP). HARBEC’s implementation of the EnMS at its small plastics manufacturing facility in Ontario, New York, enabled a 16.5% improvement in energy performance.

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